Ok, so..........
This is another of those 'I'd probably rather not share this' type posts, but in the interests of helping others, I'm going to anyway.
I'm a plonker.
You know how sometimes you think you know exactly what you're doing, to the point where you over complicate things looking for a deeper issue? Well, yes. That might be me
I may have overlooked something fairly simple!
Some time ago, as documented, the car felt like it was getting a little slower. It wasn't as aggressive, and seemed to be running very rich.
I checked everything over thoroughly, and found no leaks at any joints, no other issues, and all seemed to be OK, but it was rich, and flatter than it used to be.
Again, as documented a month or two back, I swapped from my 4 bar fpr down to a 3 bar in an attempt to lean it off a bit for my stupid (blind) ecu.
This worked, fuelling leaned out to a more acceptable level, and the car drove much better. happy days.
Now, some of you will remember, that back in July, I posted this:
It was split, but it looked like it was only through the outer ply, and it didn't appear to be all the way through at all. The car was still holding a solid 20psi, as it has done for a long time (<--take note of this bit!!!).
I contacted Jamie at Forge, who was awesome, and sent out a brand new hose the very next day:
Awesome service as usual.
So, I had the new hose, the old one didn't appear to be leaking, and I've had a lot going on lately, new job, garage build etc. the long and short of it is, I didn't fit it, and thought it could wait until I give the car a thorough going over when the Emerald goes on.
At Curborough 2 weeks ago, I was 0.6s off my PB. the car felt good, and I strung together what felt like a couple of near perfect laps. I just couldn't understand why it was slower.
Looking back through videos, I was only reaching the first or second light of 4 on my shift light in 3rd down the straight, compared to all 4 lights the previous year. This equated to roughly 400rpm down on a very short straight - Hmmmmmmmmmmmmmmmmmmmmmm
At Castle Combe last weekend, the car once again felt great, but I had real trouble trying to stick with Gurds on the fast bits, and had to work extra hard under brakes to try and stay with him around a lap.
Towards the end of the day I took Dave CC (some of you will know Dave) out for a few laps, and he instantly looked a little dissheartened at the straight line pace. It'd been a long day, and the car was starting to feel tired.
A look at the boost gauge showed it was only peaking at 16-17 psi. EGT's were good (818 peak), AFR's were OK, if a little rich.
I parked it up after the day and left it there until Saturday morning, at which point I decided to investigate.
I popped the bonnet, and immediately went to check the previously tiny surface split on the charge pipe:
Hmmmmmmmmmmmmmmmmmmmmm, that looks somewhat more sinster than it did previously.
I popped the hose off as the TB, and stuck my hand down to the inside of the split:
OH.