The map I did 383bhp on was different to this one and was tweaked according to the setup at the time, it was a stage after the current one as I had an issue with overboosting (N75 pipe issue) and MAF readings...
Fuelling was about right at the time but on the way to the dyno the FPR pipe must have finally given up the ghost and the N75 pipe came off (again!!)... The N75 pipe was put back on and 383bhp was the result but there was still a problem as the boost gauge was only reading a little over 1bar and the injectors were close to fully on. When I looked into this, it was due to a split FPR pipe which the boost gauge is tee'd off so causing a small boost leak, lower than usual fuel pressure under boost (rising rate regulator) and incorrect reading on the boost gauge. Fuelling was tweaked to suit and once the pipe was fixed meant that the tweaked map was overfuelling so reverted back to a previously known working map and all was ok.
My new exhaust has made things a little leaner off boost but still not sure why its dumping fuel. Its totally possible that the current map is still a way off with all the little red herrings we have encountered while mapping so before doing anything else I am going to give the car a once over making sure all pipes are sound with no boost or vacuum leaks before proceeding with the next round of mapping.
Its possible the ECU is falling back on protection maps as there are so many sensors and variables that control a std ECU thats its difficult to know what the ECU is actually doing sometimes...
I went over to Ajec knowing that the map wasn't the finished one but was hoping to get some good logs from it to see what needed tweaking to get it finished... the fuel dump is a new one and on the way back from Ajec, my boost is now showing 1.4bar... Testing the actuator leads me to believe that its now relaxed a bit as its opening at 12psi (0.83bar) which is a little less than the 1bar its rated at. This is fairly typical and the 1.4bar I am seeing on the gauge is actually correct as this is what the map is requesting.
The map had a lower requested boost set as it was overboosting to over 2bar which was due to the N75 pipework, now its sorted and the actuator was relaxed a tad, it needs putting back up to 1.8bar in the map which will happen when Bill gets a chance to spend some time on it.
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